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It's been a long time coming but we finally made some dyno pulls on the
351C test mule! The short block is a standard performance rebuild of a
351C with the following parts:

Ford 351C block, 0.030" over (4.03" bore), 2 bolt mains, block did not
require a re-bore as it had low miles since last being bored and was in
good shape (no ridge), block was decked to clean up gasket surface
Pioneer brass freeze plug set
TRW L2379F forged flat top pistons with dual valve reliefs
Ford 351C forged steel connecting rods (5.78")
Ford 351C nodular iron crankshaft (3.5" stroke)
Powerbond SFI balancer
Ford Motorsport double roller timing chain (French Renold chain)
Melling M84AHV mechanical high volume oil pump
Ford Motorsport M-6005-A351 heavy duty chrome moly oil pump driveshaft
Ford 351C passenger car front sump 5 quart oil pan
Weiand 8209 aluminum 351C water pump
MSD 8480 distributor (mechanical advance, large cap)
Crane steel distributor gear (p/n 52971-1 for 351C with .531" shaft dia.)
Cometic head gaskets (p/n C5871-040 for a 4.1" bore 351C/351M/400)
FRPP M-6500-S58 "Early Block Hydraulic Roller Lifter Set". These are
Crane p/n 36532-16 link bar retrofit roller lifters but were a little
cheaper under the Ford Racing part number.
Trend custom length push rods (for the taller roller lifters)
Hastings moly rings (351C stock replacement)
Clevite rod and main bearings (Std/Std)
Crank treated to a light polishing
Clearances are .0025" on rods and .0027" mains
Fuel pump block off plate (dyno providing the fuel flow)

The engine was assembled by Dave McLain of McLain's Automotive who is also
providing the dyno services. The reusable Cometic head gaksets were provided
by Alex Denysenko of MoneyMaker Racing. The block and iron heads and intakes
were painted by Mike McDougal. For this first round of tests, the CHI 3V
225cc cylinder heads and matching Scott Cook dual plane intake were provided
by Phillip de Cadenet and the CHI 3V single plane intake was provided by
James Kayser. Short block was provided by me. Many more people have
contributed parts or cold hard cash to this effort, so I'll have a lot more
people to thank in the installments to follow.

The camshaft is from Reed Cams in Georgia and is a custom hydraulic roller,
specifically part number 535-TM280HR-284HR-107A, and is ground on a standard
base circle steel core. In picking the cam specs, we were after a street
performance grind that would have a horsepower peak near 6000 RPM with a best
shift point of 6500 RPM, a wide mid-range torque band and some idle rump-rump.
We also wanted a cam that would work well with all the heads to be tested
which range from open chamber 2V iron to Ford Motorsport aluminum high ports
to CHI 3V's. We chose a hydraulic roller to avoid the lobe and lifter wear
problems associated with the low ZDDP content associated with current
automotive oils. Also, I'm a lazy street guy and setting lash on a solid
cam is a bit of a chore in a Pantera. The cam specs are:

228/232 degrees @ 0.050" lift (280/284 @ 0.006"), 0.588"/0.588" lift,
107 LSA, 68 degrees overlap, installed in the engine on a 104 intake
centerline.

The 68 degrees of overlap should put us in the right ballpark for a
street performance cam in an engine of 351 cubic inches, considering
our relatively large intake valves. I picked the lobe separation angle
using David Vizard's cam selection guidelines. Theoretically, for this
combination of bore, stroke, intake valve diameter, compression ratio
and overlap, this LSA should give us the best area under the HP curve
(not necessarily the best peak HP). For our valve diameters, Vizard's
guidelines suggest very large lift (between 0.615" to 0.766") with the
caveat that lift be limited to whatever is consistent with the longevity
goals. Since our goal was a street engine, we went with a relatively
modest lift of 0.588".

Dave originally mocked the engine up using a borrowed set of Crane link
bar lifters. I also wanted to test the Sherman Racing hydraulic roller
lifters. Those lifters are modified OEM Ford lifters that others had
provided others with a 400 RPM increase. However, it turned out we were
unable to use the OEM Ford, Sherman Racing or Comp Cams link bar lifters
in our particular block. Due to the way this block had been machined,
at maximum lobe lift, the oil groove on the lifters is pushed up into
the chamfer at the top of the lifter bores. If we tried to run it this
way, it would dump oil pressure. There are three ways to fix this.
One is to reduce the base circle of the cam so the lifter is lower in
bore. The second is to use a lifter with a lower oil groove location
and the third is to bush the lifter bores with taller sleeves. Dennis
at Reed Cams said that, as a rule, irrespective of how much lift that
a camshaft has, the lifters generally all stop in approximately the same
location at the top, unless the base circle is deliberately reduced which
might cause problems at the other end of the lifter bores. We decided to
go with the Crane link bar lifters since they have their oil hole in a
lower location on the lifter body.

The first cylinder head and intake combination to be tested was the CHI
3V 225 cc heads coupled with a Scott Cook aluminum low rise dual plane.
Both parts are imports from Australia and are very nice castings. Scott's
intake manifold looks much like a Ford cast iron DOAE-9424-L dual plane
but is cast in aluminum, slightly taller (around 10 mm or a bit more
than 3/8") with smaller ports that are sized to fit either the CHI 3V
heads or a 4V head with stuffed intake ports (raised floor). Compression
was a little under 10:1 with the CHI heads. All pulls were made on 93
octane (midwest winter blend) pump gas and, unless otherwise noted, all
pulls were made through mufflers. Also, the atmospheric conditions were
measured and all dyno numbers corrected to standard day conditions.
The headers for the first pulls were Hooker Competition units with 1 3/4"
diameter by 27" long primaries, 3" diameter by 8" long collector (probably
part number HOK-6920HKR for 4V heads in a '67-'68 Mustang). Mufflers
were Magnaflow 3" inlet and outlet. The dyno carb was a Holley 950HP
(without air cleaner or inlet bellmouth) and we had an Innovate LM1 wide
band O2 sensor keeping an eye on the air-to-fuel ratio. The engine had
been previously run in for around an hour to seat the rings. It was run
for a few minutes to warm the oil to operating temperature and the initial
pulls made to set the total timing. Total timing settings from 32 to 38
degrees were tried. Unlike our previous dyno tests of a 10:1 compression
408 cubic inch Cleveland with closed chamber iron heads which made it's
best power at only 32 degrees of total timing, this engine made it's best
at 38. However, some trace detonation was detected by the knock sensor
in the mid range. Rather than re-curving the distributor at that time,
we opted to pull the total timing back to 33 to 34 degrees. We lost
around 5 HP but gained some safety margin.

Before the first recorded pulls, Dave guessed we'd make around 400 HP
with the dual plane and pick up 20 HP with the single plane. Sure enough,
the Cook dual plane intake/CHI 3V combo made right at 400 HP and 400 ft-lbs
of torque. This dropped to 395 HP with the timing set back. Switching to
the single plane CHI 3V intake manifold picked up 20 HP, just as Dave had
predicted. The pulls were started at 3000 RPM and the HP peaks were near
6000 RPM. We ran both intakes to 6500 RPM and the horsepower stayed
constant with no signs of dropping off. With the previous 408C which used
the same dual valve springs, horsepower began dropping at 6000 RPM no matter
whether we used the link bar Crane lifters or the OEM Ford lifters. Both
of the initial test combos had nice flat torque curves that hung around
400 ft-lbs so I think we guessed right on our cams specs. The CHI single
plane looked to have the edge from around 3000 RPM on up but the CHI is a
rather tall intake that won't fit a lot of places the low rise Cook intake
will. The Cook intake also has the edge in the sleeper department. Paint
it with some dark Ford blue and no one would know it's not a cast iron Ford
intake. Interestingly, the Cook dual plane did not have the distinct dual
resonant peaks the dual planes on our previous 408C exhibited.

We next tried a set of large tube Econo Altered drag headers which have
2 1/8" primaries of around 40 inches length and long 4" diameter collectors.
These were run without mufflers. Our mild street 351C was just not enough
engine to make use of these headers. They lost a whole bunch of torque and
didn't catch up until 6000 RPM. We then tried a set of Pantera 4-into-1
headers (Hedman style with 2V port openings). These have rather short
primaries (between 19" and 24") of 1 3/4" diameter and a tiny collector with
2 1/4" outlet. They lost maybe 15 ft-lbs but closed the gap some as RPM went
up. Overall, I don't think they worked as well on this engine as the Euro
GTS style Pantera headers had on the 408C. Those headers have a 2" primary
with similar short primaries but have a tri-y type collector. It would be
interesting to experiment with a better collector on the Hedman headers to
see what sort of improvement can be made. The stock Pantera ANSA mufflers
were just plain terrible. Just as the Euro GTS mufflers had on the 408C,
the stock Pantera mufflers lost 50 ft-lbs and 50 HP to the 1 3/4" long
tube Hookers with 3" Magnaflows. Anyone got a set of 1 7/8" primary long
tubes to lend us? 1 7/8" might be better on this engine.

We attempted to try a small 4180 Holley (CFM rating in the 585 range) to
see how much HP we would lose with the reduced carb flow but we ran into a
delay. The 4180 uses a different style bowl gasket which we didn't have
on hand. As we hadn't had anything to eat or drink since breakfast, we
decided it was a good time to knock off for the day. Dave noted that,
given the number of pulls we made, it looked like the engine had pretty
decent fuel economy. I also opined that the torque band should be a good
match to the gearing of the Pantera. Dave said he'd pick up the 4180
gaskets and we'll give that a try later. Also, we plan on trying 1.65:1
roller rockers on the exhaust side before moving on to the next set of
heads. We may also try the Parker Funnelweb on the CHI 3V heads if the
port mismatch is reasonably close.

Dave has the specifics of all the pulls recorded on his shop PC, along
with the cylinder head and intake manifold flow bench results. When he
sends those to me, I'll enter them into a spreadsheet and update this
post with the relevant data.

Dan Jones
Original Post

Replies sorted oldest to newest

Dan,

All good stuff.

I think it won't be long before you're banging on the 500bhp door.

I really looking forward to you guys testing my little 4180, a highly underated little carb. I'm sure it will be fine on a bone stock Cleveland offering reasonable perfomance down stairs and great mileage.

Do we worry about that in a DT?

Phil
79 Longchamp GTS 3061
> Bravo Dan and Dave!
>
> Thanks for all your efforts Dan. This makes for very interesting
>reading. I look forward to the next instalment!
>
> All good stuff.

Thanks guys. It's going to be fun.

> I think it won't be long before you're banging on the 500bhp door.

Dave's dyno is a unit that he built using a Land and Sea absorber,
electronics and software. It's on wheels so it can be rolled in
and out of the shop. We do the pulls under a car port type awning.
The dyno is know to be 4 to 5% conservative when comparing the same
engine on his dyno and the dynos used for the Engine Masters Competition,
at Competition Cams and at Bill Mitchell's. Also, Dave doesn't use the
automatic correction. Instead, Dave enters the atmospheric data manually
from a weather station and no inertial correction factor is used. With
these variables, dynos can vary by 10% very easily. If we take our best
single plane pull from the first day (416 HP), add the 5 HP we lost from
pulling back on the timing and then increase it by the known 5% correction
factor, we'd end up with 442 HP. However, I'm not too concerned about the
absolute numbers. It's more important to see what the relative changes
are between different parts.

> I really looking forward to you guys testing my little 4180, a highly
> underated little carb. I'm sure it will be fine on a bone stock
> Cleveland offering reasonable perfomance down stairs and great mileage.

I think it would work very well on a stock 351C. I was hoping to test
it on the relatively stock 351C in my white Pantera but didn't get a
chance to try it before the snow started falling. It will be interesting
to see what the dyno says. Given the HP difference between the dyno carb
and the 4180, I should be able to predict where the carb will start to
be a restriction.

> Do we worry about that in a DT?

Not too much, though I recently took a 900 mile trip in the Pantera.
Fuel economy was right around 20 MPG, IIRC. Luckily, fuel cost had
dropped to $1.37 per gallon. The recent drop in prices is very
welcome as the dyno is a 200 mile round trip.

Dan Jones
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