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I wish I was making this up but unfortunately not.

Started the car as normal to let it warm up and after 10 seconds it sputtered and died.  Went to start it again and it was seized.  Thought it was the starter so put it in gear and rocked the car back and forth.  This un-seized the engine so I started it again and it ran but I could hear something rattling inside the engine.

Turns out the air filter all-thread bolt (~3") sheared off at the base of the carb and unthreaded from the top wingnut then fell down into the intake.

At this point I can't find the bolt with a bore scope or magnet.  I tried using a brake bleeder vacuum tool last night in all of the cylinders with no luck.

With all the plugs removed it spins fine and doesn't seize. I would say every 2nd rotation I feel a slight binding in the engine.

I don't want to pull the intake if I don't have too but that may be the only option.  The engine will run but I don't want to create any more damage.

Any ideas if it would be above the valve train or has it probably dropped into the cylinders?

I haven't tried removing the exhaust to see if it's been passed thru there. 

Any help is greatly appreciated.

My new year's resolution is to prevent the rear deck from pushing against the air cleaner due to the mid-rise Speed Master intake.  I'm sure this is the root cause.

Thanks,

John

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Thanks Simon,

I will try the compression test first.

I have a flat tappet ISKY cam if that makes a difference?  What am I looking for on the valve caps and is that checked down inside the intake? 

I can see inside the middle intake runners but can't see much in the outer 4 cylinders due to the longer intake runners and the curvature of the intake.

John

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  • mceclip0

...'IT's' IN a Cylinder!! The Thud was The Piston Bending a Valve as the Stud Tried to pass Under, or Jamming a Piston. That is what Stopped the Engine...and You tried to restart. You're Going to have to Pull the Head(s). There will be Great Damage. In My View. Anything 'inside' the Air Filter, can come loose. Why Holley Leaves out 2 Screws in their Baseplates, and Why I Never place a Washer Under the Wingnut!! I Feel Your Pain!

Doing a 'Compression Check' means turning over the Engine. Enough Damage!

Happy New Year

MJ

Last edited by marlinjack

when the sparkplugs are out of the heads , you also can turn loose the valve rockers till the springs are decompresed, use a pressure airgun into the sparkplug holes , when there is one leaking than there is the problem.

this way it is not needed for turning  the engine for protect further damage.

maybe you have luck and find the problem with a flexible magnet.

but most of the time there is a valve bented and one head needs pulled from the engine.

good luck,

Simon

There is no way you can do this without at least partially pulling the engine apart and you should not turn the engine over further unless by hand. You may be lucky and as it's 3" the stud is caught in an intake valve, but as Marlin said the seize was likely due to the piston hitting the valve, so at a minimum expect a bent valve or pushrod and potentially damaged piston and possibly bent rod. Only way to confirm is start pulling it apart. I'd pull the intake and rocker covers first to look in the runners and at the pushrods / rockers and see where it binds turning over by hand.

But honestly that is all just an autopsy attempt, if it were me I'd just pull the engine and strip it down.

Last edited by joules

I pulled the intake off and didn't see anything on the top side of the valves nor any scratching or scoring.

I decided to drain the oil and to my surprise at least 1 gallon of straight green anti-freeze came out, no milky oil at all.  I dumped the anti-freeze and went to drain it again then the oil, milky came out.

Last oil change was 1K miles ago.

At this point, I'm thinking a cracked block or somehow punched a hole in the aluminum heads?   These are Speed Master 3V heads for reference.

Engine is coming out but curious of the root cause of the failure.

Thanks,

John

IMHO, allthread is evil and should NEVER be used for air cleaner studs!!!!   It isn't hardened at all........  Unless it was in the previous build, having it on the carb for only 4K miles should tell you how inadequate this material is to use in this application.....as a carb stud!

If this 3" piece is still in an intake port/valve you should be able to see it with one of those camera on a snake deals.....go in thru intake ports and or spark plug holes.....but with antifreeze in your oil.....your future task list seem obvious! Just a matter of which head comes off first......

BUMMER BIG TIME!  Hope it turns out to be salvageable!

Steve

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